1. The field technicians were dispatched to the site to investigate.
• The oil level gauge was confirmed to be functioning properly, and no evidence of oil leakage was observed.
2. During the fault event, the feeder protection relay also indicated a ground fault, suggesting the transformer may have experienced an internal fault to ground.
3. A Dissolved Gas Analysis (DGA) was performed, and results showed elevated gas levels, consistent with internal electrical faults.